@xingxing wrote:
my RC plane installed pixhawk is out of control after take off ,the good news is the entire process has been record included camera and osd video except telemetry log ,please find the detail crash below:
i switched to manual mode and increase throttle for take off ,then switched to FWBA mode after the wheel off ground .I try to make a left turn ,but the plane do not response to my controller input .then I realize the problem and switched RTL mode immediately ,but the plane keep flying without come back home .the GPS locator help me to get back the plane .the dataflash log can be find in the below link:
data flash log
please go to YouTube visit the camera video
runcam camera
OSD CAMERAHope some one can help to find out the issue this time,thank you for all your attention.
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